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WA9302A-LR 960604G EOrECHNICAL E NGINEERING E NVIRONMENTAL 10046 Monroe Drive Dallas, Texas 75229 GEE Consultants, Inc. · (214) 352-5433 · Fax (214) 352-6972 PIER INSPECTION REPORT Report Date: Cliem: Project: Identification: Method of Test: June 4, 1996 City of Coppell Village Parkway Pump Station Add. Piers Inspection Visual Inspection Inspection Date: May 31, 1996 Pier Inspection Report No.: 3 Page Number: Page 1 of 1 Project Number: 96-0172 Pier # B-3 C-3 SW-1 SW-2 SW-3 SW4 SW-5 SW-6 Shaft Size 18" 18" 18" Depth to Bearing Strata 22' 7" 23' 0" Req'd Actual Total Bearing Casing Pent. Pent. Depth Material Depth 8' 0" 9' 0" 31' 7" Shale 21' 10" 8' 0" 8' 0" 31' 0" Shale 21' 4" 10' 0" Dark Gray Clay N/A 10' 0" Dark Gray Clay N/A 10' 0" Dark Gray Clay N/A 10' 0" Dark Gray Clay N/A 8ft 10' 0' Dark Gray Clay N/A Remarks Mr. Larry Davis - City of Coppell Mr. Gary HeMticks - Shimgk, Jacobs and Finklea Our letters and relx~.s are for the exclusive use of the client to whom they are nddrus~. Dry, clean, plumb Dry, clean, plumb Clean, 5" of water pumped out before placing concrete Dry, clean, plumb Pier bottom started caving in with water, so they were backfilled until okayed by structural engineer. Pier bottom started caving in with water, so they were backfilled until okayed by structural engineer. Pier bottom started caving in with water, so they were backfilled until okayed by structural engineer. 10' 0" Dark Gray Clay N/A Pier bottom started eaving in with water, so they were backfilled until okayed by structural engineer. w t~n app I. Our l~ttara and reports apply only to th~ sample t~st~l and/or i~p~ct~d, and arc not r,~cessariJy indicative of th~ qtintiti~l of appa~ntly id=ntical or similar pt~dli;ls.