Loading...
Hammond- PN140529 (3)EXISTING STORM PIPES DETENTION REGRADE DETENTION POND DRANAGE PROVIDE EQUIVALENT VOLUME DITCH OF EXISTING DETENTION POND PROPOSED POND OUTFALL 1.25 8.5 EX FH WAS— r PROPOSED ALLEY4 . --�- .. — ACE GARAGE II GARII GARAGE t II GARAGE II GARAGE I GARAGE r GARAGE r GARAGE � GARAGE i GARAGE 'I GARAGE I' GARAGE (I GARAGE GARAGEGARAGE GARAGE ,GARAGE _ GARAGE LOT 1 LOT 17E E I I I GARAGE PORCH LOT 2 LOT 16 I I I LOT 1 LOT Y LOT 3 LOT 4 LOT 5 LOT 6 LOT 7 LOT 8 LOT 9 LOT 10 LOT I I I LOT 11 12 LOT 13 LOT 14 LOT 15 LOT 1X Z PORCH F=. I I PORCH PORCH .PORCH PORCH PORCH PORCH PORCH I PORCH PORCH PORCH PORCH PORCH PORCH PORCH PORCH A I I EXISTING STORM PIPE 7.4 EX INLET EX STM MN l• ® EXISTING POND OUTFALL TO BE ABANDONED EX F-bia.- HMOND STREET EXISTING STORM PIPE EX INLET -... EX INLET EX INLET — — III Q� i • IJI jr i 30 •0 •i GRAPHIC SCALE 1"=30' at 24"x36" Flow Arrow -- Existing Storm Sewer Line tc (min) — Proposed Storm Sewer Line 1100 (in/hr) Drainage Divide Line 0100 (C.f.s.) Drainage Area Number A X.XX �--Acres 0.80 X. X WS) 1.09 DRAINAGE AREA CHART SHEETFLOW TO HAMMOND RECEIVED SEP 1;7.2014 PLANNING DEPART D.A. tc (min) C 1100 (in/hr) A (acres) 0100 (C.f.s.) COMMENTS A 10 0.80 8.5 1.09 7.4 SHEETFLOW TO HAMMOND B 10 0.80 8.5 1.25 8.5 PROPOSED ALLEY INLET THIS DOCUMENT IS RELEASED FOR THE PURPOSE OF INTERIM REVIEW UNDER THE AUTHORITY OF MATT KOSTIAL, P.E. NO. 88549 ON 07-01-14 IT IS NOT TO BE USED FOR CONSTRUCTION OR BIDDING PURPOSES. WINTMAI 1`111 Mill 2.4 acres CITY OF COPPELL DALLAS COUNTY, TEXAS .NT ORACLE ENGINEERING 330 Fairfax Drive Little Rock, Ar 72205 TELE (214) 226-5325 DESIGN DRAWN DATE SCALE CITY CASE # NO. MPK MPK 06/14 1"=30' -- �� at 24"x36"