Loading...
Gibbs Station 1-LR 920910 (3)ALPHA TESTING, INC. 2209 Wisconsin St., Suite 100 Dallas, Texas 75229 (214) 620-8911 DAILY FIELD REPORT TESTED FOR HEATH & KNIGHT PROPERTIES, INC. DATE DALLAS, TEXAS 09/i0/92 PROJECT GIBBS STATION LAKES OF COPPELL COPPELL, TEXAS OUR REPORT NO. 92020-41 WEATHER: OVERCAST\RA I N DATE: TEMPERATURE RANGE: 80 TO: ALPHA Representative: D. M. 9O 09/i0/92 THE ALPHA TECHNICIAN TRAVELED TO THE PROJECT SITE AS REQUESTED 8Y THE CLIENT TO PERFORM FIELD DENSITY AND CONCRETE TESTING. A TOTAL OF NINE FIELD DENSITY TESTS WERE PERFORMED ON FILL SOILS FOR THE UTILITY LINES AND BUILDING PADS. SEE ATTACHED REPORT OF FIELD COMPACTION TESTS. THE GREGORY AND C.W. YOUNG REPRESENTATIVES WERE INFORMED OF TEST RESULTS WHICH APPEARED TO COMPLY WITH PROJECT SPECIFICATIONS. IN ADDITION, THE TECHNICIAN CAST ONE SET OF FOUR CYLINDERS FROM CONCRETE PLACED FOR THE MANHOLE AT STATION O+OO, LINE 'D' ON THIS DATE. THE C.W. YOUNG REPRESENTATIVE WAS INFORMED OF ALL TEST RESULTS. CONCRETE COMPRESSION TEST RESULTS WILL FOLLOW ON A SEPARATE REPORT. THE TECHNICIAN ALSO 08SERVED THE PROOFROLLING OF LOTS NUMBERED 42, 41, 40, 39, 38, 37, AND 36 OF 8LOCK "E" THE AREA WAS EXCAVATED TO THREE FEET BELOW EXISTING GRADE. SOME AREAS WERE EXCAVATED TO FIVE FEET BELOW EXISTING GRADE DUE TO WEAK SOIL ENCOUNTERED AT THREE FEET. THE ENTIRE AREA WAS PROOFROLLED USING A MOTOR GRADER. NO SOFT OR WEAK AREAS WERE ENCOUNTERED. TECHNICIAN RETURNED TO THE LABORATORY UPON COMPLETION OF SCHEDULED TESTING.