Loading...
Gateway BP(2.5)-LR 981217 Information BuiM On Engineering · ConsuLting · Testing REPORT OF FIELD COMPACTION TESTS TESTED FOR: ALAN GRIMES ROGERS O'BRIEN CONSTRUCTION 11145 MORRISON LANE DALLAS, TX 75229 PROJECT: G & K LAUNDRY PROCESSING DATE: December 17, 1998 OUR REPORT NO.: 337-80080-58 TESTDATA: (42) FLEX BASE OPT. MOIST. = 11.0% MAXIMUM COMMENTS' TEST TEST SOILID LABDRY * WATER WET PERCENT Spec. 95% Min NO. DEPTH ELEVATION NUMBER DENSITY CONTENT DENSITY DENSITY COMPACTION 1 B/S FINAL 42 124 . 5 14 . 6 136 . 7 119 . 3 95 . 8 3 A TEST LOCATION: NORTHEAST ENTRYWAY 1 RETEST OF TEST #1 TAKEN ON 12/16/98 __ NOTES: 6. OTHER * (42) ASTM D1557 TEST INSTRUMENT: TROXLER, 3430, 20950 REMARKS: PSI did not monitor the material placement. TESTS PERFORMED PER ASTM D2922-96 & ASTM D3017-88(93) *COMMENTS: 1. FILL MATERIAL A. TEST RESULTS COMPLY DENSITIES SHOWN: Lbs per cubic foot 2. BACKFILL B. PERCENT COMPACTION DOES NOT COMPLY WATER CONTENT: Percent of dry weight . 3. BASE COURSE WiTH SPECIFICATIONS PERCEN.T C .O. MPACT O.N BaseD.on m. axi. mu..m Dry 4 SUBBASE C. RETEST OF PREVIOUS TEST oensky obt.aineo on sample inDicateD Dy 51 SOIL CEMENT D. MOISTURE N EXCESS OF SPECIFICATIONS soil ID numDer. E. MOISTURE BELOW SPEC FICATIONS STANDARD COUNT M: D: ADJUSTMENT DATA M: D: TECHNICIAN: J. ASTIZ Respectfully submitted, Professional Service Industries, Inc. cc: (1) ROGERS O'BRIEN (1) HALFF ASSOCIATES, INC. (1) CITY OF COPPELL Attn:GARRETH CAMPBELL THESE TEST RESULTS APP~ ~LY TO THE SPECIFIC LOCATI~S NOTED ANO ~Y NOT REPRESENT ~Y OTHER LOCATI~S ~ ELEVATI~S. REPORTS ~Y NOT BE REPR~UCEO, EXCE~ IN F~L, ~THOUT ~I~EN PER~SSI~ BY PR~ESSIOt~AL SE~ INDUSTRIES, INC. PSI A-100-214)F Professional Service Industries, Inc. · 2556 Gravel Drive · Fort Worth, TX 76118 · Phone 817/284-3783 · Fax 817/284-8942