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WA9302-LR 960206 (8)'EOTECHNICAL E GEE Consultants, Inc. E I NVIRONMENTAL 2540 Glenda Lane · Suite 108 · Dallas, Texas 75229 · (214) 620-9791 · Fax (214) 620-9794 REPORT OF CONCRETE MIX INSPECTION Report Date: February 6, 1996 Date Concrete Placed: January 16, 1996 Standard 6"x12" Client: Natgun Corporation Area 28.27 Square Inches Project: 6.0 Million Gallon Water Storage Tank Concrete Report No.: 139 Contractor: Natgun Corporation Project No.: 95-0258 Concrete Supplier and Plant: RediMix Concrete - Plant #1 Location of Placement: Wall Panel MATERIALS So~e~ ~a~ W~. INSPECTION DATA Description (Lbs ./Cu. Yd) Mix Number: Time Sample Batebed: 12:38 pm Cement: Time Sampled: 2:15 pm Fly Ash: Sample Location: WC-6 Truck/Ticket No: 129/18227 Cearse Aggregate: Temperature: Intermediate Aggregate: Ambient Range: 63°F Fine Aggregate: Concrete Range: 69°F ACmixtures: Slump Range (inches): 5~A'' 1 Weather Conditions: Parity Cloudy Time Started: 8:15 am 2 Time Completed: 4:30 pm Added Water: 15 gal. Sample Air Content (%): 5% Total Cubic Yards Placed: 46 C.Y. Required Strength (Lbs./sq.in.): 5,000 psi Specimen Measured Age Date Total Load Compressive Strength Number Slump (in.) (Days) Tested (Lbs.) (Lbs./Sq. In.) Remarks CWT 479 51/2" 8 01/24/96 164,280 5,810 Slump before super plasticizer was CWT 480 51/2" Hold Hold 11/2" CWT 481 51/2" Hold Hold est Methods Utilized Fracture Regular STM C-31,C-39,C-143 (Unless Noted Otherwise) Cylinders Made By: P.C. Remarks and/or Distribution: cc: Mr. Larry Davis - City of Coppell Mr. Bob Barbarisi, Jr. - Natgun Corporation Mr. Gary Hendricks - Shimek, Jacobs and Finklea Ggg ~, Ira:. Reviewed by: