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Northlake 635(7)-LR 980529 Project: Calling Center Report No.: 9813836 Coppell, Texas Date of Service: 05/29/98 Project No.: 43-1279-97 Technician: B. Otis Page: I of l Pier Identification D.4 D.6 D.8 E.6 E.8 J.9/5.3 K/5.3 K/5.6 I Pier Diameter (in.) 24 24 24 24 24 24 24 24 ~ Bell Diameter (in.) 54.0 54.0 54.0 54.0 54.0 48.0 48.0 48.0 Top of Pier Elevation (ft) 97.0 97.0 97.0 97.0 97.0 94.0 94.0 94.0 Req. Depth From Exist. Grade (ft) 12.0 12.0 12.0 12.0 12.0 12.0 12.0 12.0 Initial Depth of Pier From Existing Grade (ft) 15.2 15.5 15.2 15.2 15.2 14.4 13.5 13.5 Final Depth of Pier From Existing Grade (ft) 15.3 15.6 15.2 15.3 15.4 14.5 13.9 13.5 Depth From Top of Concrete (ft) 14.3 14.6 14.2 14.3 14.4 13.0 12.4 12.0 Condition of Bottom (wet or dry) DRY DRY DRY DRY DRY DRY DRY DRY Plumb Within Tolerance (yes or no) YES YES YES YES YES YES YES YES Casing Diameter (in) N/A N_/_A_ ...... N/A__ _N/A N/A N/A N/A N/A __ j _.__Cased De__P_th !ft! .............. N/A N/A N/A N/A N/A N/A N/A N/A Number of Vertical Bars (ea.) 6 6 6 6 6 6 6 6 Reinforcing Bar Size (#) 6 6 6 6 6 6 6 6 ._ Length 0f.Ve~!_ca/__B.._a_~__(ff._! 16.0 16.0 16.0 16.0 16.0 14.0 13.0 13.0 Time Drilling Was Completed 12:00 AM 09:08 AM 09:16 AM 09:28 AM 09:53 AM 02:00 PM 02:20 PM 02:45 PM Time Concrete Was Placed 11:30AM 11:35AM 11:40AM 11:50AM 03:05 PM 03:20 PM 03:28 PM 03:36 PM ENGLNEERING, INC. 8901 Carpenter Frwy., Suite #100 Dallas. Texas 75247 Date of Service: 05/20,"1998 Report No.: 9813362 Report Date 05/29/1998 Client No.: 71765000 Project No.: 43-2479-97 Client: Prentiss Properties Limited, InC.Attn: David Glass Project: Calling Centercoppell, Texas COPy 3890 W. N.W. Hxx3,, Suite 400 Dallas TX 75220 Services: Structural steel :nspection. On this date, an HBC Engineering reTresentative arrived an The above referenced jobsite as scheduled fcr steel framing insoecnion. The following items have been visua!lv ~ = ~--~ 1. Refer to Report ~9809759, daned 04/15/98 iuem ~3 and %4. A representative sample of joisn and girder tails have been insDected cn this date with the fo!icwinu results: a. Girder to panel tails not %-:elded (refer nc 06/S3.1}. b. 3oi=- tail angle non welded at Grid Lines E-8. Siau has non been removed frcm welds prior ~ ~;isual inspection (this ccndinion does non ccmply winh AWS Dl.!-98). 2. Refer tc Report ~9809759, da5ed 04/15/98 ilem %1: a. Jois5 seau 5o panel ccnnection has been repaired per attached sketch wi~h exception; non-shrink grout has nc5 been placed. ~ Isem %u on Report ~9809759, dazed 04/i5/9~ has nct been resolved. Technician: Royce Tomlin ~ Engineering, Inc. Report Distribution: (1) Premiss Properties Limited, Inc. (l) Halft'Associa:cs, [nc. (1) Butler Construction (1) City ot'Coppel! Paul D. Smith, P.E. (1) Alliance Architects, Inc. (1) HCBeck Contractors Senior Project Engineer (1) Brockette Davis Drake, [nc. (1) City of Coppcll This report is exclusively for the use of the client indicated abox e and shall not be reproduced except in full without the xwitten approval of HBC Engineering, Inc. 99MP Page ! of I