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Northlake 635(5)-LR000127irk-PLACE DENSITY T~,~TING INGINEERII\K', INC. a division oj~rerrat:on 8901 Carpenter Frwy., Suite #100 Dallas, Texas 75247 Date of Service: 01/11/2000 Client No.: 85229000 Client: Transwestern Property Company Attn: James Gaspard 12221 Merit Drive, #450 Dallas TX 75251 Services: In-place density testing. CONTRACTOR: Butler Construction Report No.: 0001702 Report Date O 1 /27/2000 Project No.: 94991456 Project: Coppell Commerce Center 1221 S. Beltline (Bldg. A) Coppell, Texas PROJECT DATA Laboratory Test Method: Field Test Method: ASTM D-698 ASTM D2922 ASTM D3017 MOISTURE DENSITY RELATIONS: Maximum M/D No. Description Moisture % Density pcf t Gray & med brown clay w/tan & gray limestone 18.0 106.5 Project Requirements Moisture Density -1/+3% 95% 2 Lt. brown & tan shaley clay 22.0 98.5 -1/+3% 95% FIELD DENSITY TESTS TEST PROBE LIFT/ M/D MOISTURE DRY DENSITY DENSITY NO TEST LOCATION DEPTH ELEV No. (%) (pcf) (% max) Sanitary Sewer, Line S-1 4 Station 2+00 6' BEG 1 17.4 104.2 98 5 Station 2+00 5' BEG 1 20.5 105.5 99 6 Station 2+00 4' BEG 1 17.0 103.8 98 7 Station 2+00 3' BEG 1 20.0 105.0 99 8 Station 2+00 2' BEG 1 17.8 104.3 98 9 Station 2+00 1' BEG 1 17.0 102.9 97 10 Station 4+00 6' BEG 2 21.8 96.3 98 11 Station 4+00 5' BEG 2 21.3 94.5 96 12 Station 4+00 4' BEG 2 21.7 96.8 98 13 Station 4+00 3' BEG 2 21.9 96.2 98 14 Station 4+00 2' BEG 2 21.6 96.2 98 This report is exclusively for the use of the client indicated above and shall not be reproduced except in full without the written approval of HBC Engineering, Inc. 07SDS Page 1 of 2 Report No.: 0001702 ~"~°~ TEST PROBE LIFTJ M/D MOISTURE DRY DENSITY DENSITY NO TEST LOCATION DEPTH ELEV No. (%) (pct? (% max) 15 Station 4+00 1' BEG 2 22.3 95.4 97 16 Station 5+00 6' BEG 2 22.1 98.0 100 17 Station 5+00 5' BEG 2 23.0 96.9 98 18 Station 5+00 4' BEG 2 23.3 97.5 99 19 Station 5+00 3' BEG 2 22.2 97.2 99 20 Station 5+00 2' BEG 2 22.0 96.8 98 21 Station 5+00 1' BEG 2 22.9 95.7 97 Storm Sewer 22 Line D, Station 3+00 Final 2 21.9 98.4 100 23 Line D, Station 1+50 Final 2 22.3 97.6 99 24 Line E, Station 2+00 Final 2 23.0 98.0 100 25 Line C, Station 3+00 Final 1 18.3 108.1 102 Test results on this report meet project specification. BEG = below existing grade Field Results Reported To: Contractor E gin 'ng, Inc. Technician: Roy Montgomery Started: 9:30a Finished: 11:30a Report Distribution: (1) Transwestern Property Company (1) City of Coppell (1) O'Brien & Associates (I) City of Coppe6 Paul D. Smith, P.E. (1) Technistructures, Inc. Senior Project Engineer (1) Butler Construction This report is exclusively for the use of the client indicated above and shall not be reproduced except in full without the written approval of HBC Engineering, Inc 07SDS Page 2 of 2