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Callahan-LR021118i r~ FAROO CONSULTANTS, INC. REPORT OF FIELD COMPACTION ] 1440 Reeder Rd. • Dallas, TX 75229 Tel. (214) 352-4100 • Fax (214) 352-4811 Tested For: Bonner Associates Date Performed: 11-18-02 Project: Callahan Addition FCI Project No.: M02-412 Coppell, Texas Density: Per ASTM D-2422 Gauge Manuf.: Humboldt Moisture: Per ASTM D-3017 Gauge Model: HS-SOOIEZ Test Mode (DT / BS): DT Probe Depth: 6 inches MOISTURE/DENSITY RELATIONS Proctor No. Material Description Optimum Moisture % Maximum Dry Densit PCF 1 Dark Brown Clay 23.0 101.0 IN-PLACE TEST RESULTS Test Elevation or Location Proctor Percent Dry Density Percent No Lift No. Moisture PCF Density 46 FG-1' Sanitary sewer line, 30' west of building pad 1 24.2 95.9 95.0 47 FG Sanitary sewer line, 35' west of building pad 1 23.0 98.0 97.0 (R) AFTER TEST NUMBER INDICATES RETEST (F) IND]CATES FAILURE TO COMPLY WITH PROJECT REQUIREMENTS Technician: Dan Ratty, EIT Checked By: _~~ Distribution: Bonner Associates -Paul Pitts City ofCoppell -Rick Odell C3 Contractors -Taylor Barnes LIMITATIONS: The teu results presented herein wet~e prepazcd based upon the specific samples provided for resting. We azsutne no responsibility for variation in quality Icomposiiion, appem~ance, pn'foimance, etc.) or any other failure ofsimilm~ subject matter provided by persons or conditions over which we have no control. Our Ict[ers and reports are for the exclusive use of the client's to whom they are addressed and shall not be reproduced except in full without the written approval of Fargo Consultants, Inc. Consu/ting + Geotechnica/ Engineering + Construction Mate~ia/s Testing