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Bank One-LR030829REPORT OF IN-PLACE DENSITY TESTS Report Number: 94031289.0023 Service Date: August 20, 2003 ']Ferracon 8901 Carpenter Frwy, Ste #100 Dallas, Texas 75247 (214) 630-1010 Client: Bank One Texas NA Attn: Danny Buckner 8111 Preston Suite 250 Dallas TX 75225 Report Date: August 29, 2003 Project: Bank One - Coppell TX 616 North Denton Tap Rd Coppell, TX Project Number: 94031289 Services: In-place density tests. On this date, HBC/Terracon's technician arrived at the above referenced jobsite as scheduled for in-place density tests. After arriving at the jobsite, HBC/Terracon's technician was notified that in-place density tests were cancelled due to the contractor was not ready for testing. Technician: James L. Atnip Report Distribution: (1) Bank One Texas NA (1) City of CoppeJl TX (1) Aguirre Building Systems (1) City of Coppel[ TX Reviewed by: HBC/Terracon Husse~n H Abusaad, P.E Senior Project Manager The tests were performed in general accordance with applicable ASTM, AASHTO, or DOT test methods This report is exclusively for the use of the client indicated above and shall not be reproduced except in full without the written approval of Terracon Test results transmitted herein are only applicable to the actual samples tested at the location(s) referenced and are not necessarily indicative of the properties of other apparently similar or identical materials REPORT OF DRILLED PIER OBSERVATION Report Number: 94031289.0020 Service Date: August 18, 2003 lrerracon 8901 Carpenter Frwy, Ste #100 Dallas, Texas 75247 (214) 630-1010 Client: Bank One Texas NA Attn: Danny Buckner 8111 Preston Suite 250 Dallas TX 75225 Report Date: August 29, 2003 Project: Bank One - Coppell TX 616 North Denton Tap Rd Coppell, TX Project Number: 94031289 **REVISED Services: Drilled pier observation. On this date, HBC/Terracon's technician arrived at the above referenced jobsite as scheduled for drilled pier observation. See the attached sheet(s) for recorded data. NOTE: **Pier 19 was concreted half way, then the casing was removed because there was no concrete to place into the pier hole and the next concrete truck would arrive at the jobsite for two hours. HBC/Terracon's technician informed the superintendent that all the water and mud needed to be pumped out of the pier hole before the the rest of the pier hole could be concreted. The contractors did not pump the water and mud out of the pier hole. The concrete was placed with the mud and water still in the pier hole. The first truck of concrete filled the pier hole to within approximately 9 feet from the ground level. The superintendent was notified that the contractors had not pumped the water out of the pier hole before the second truck of concrete was placed. **This repod has been REVISED on 08~29~03 by changing the Time Concrete was Placed for Piers 4 and 19 (see attached sheet). Technician: Wesley A. Lawson Report Distribution: (1) Bank One Texas NA (1) City of Coppell TX (1) Aguirre Building Syslems (1) City of Coppel[ TX Reviewed by: Husse~ HYAbusaad, P E Senior Project Manager The tests were performed in general accordance with applicable ASTM, AASHTO, or DOT test methods This report is exclusively for the use of the client indicated above and shall not be reproduced except in full without the written approval of Terracon Test results transmitted herein are only applicable to the actual samples tested at the location(s) referenced and are not necessarily indicative of the properties of other apparently similar or identical materials Page 1 of 1