Loading...
SS9402C-LR 980714Compaction Test Report Patton, Burke & Thompson 10555 Newkirk Street Suite 530 Dallas, Texas 75220 CLIENT: CJ~t~ OF COPPELL 225 PARKWAY BLVD. P. O. BOX 478 COPPELL, TEXAS 75019 O7/14/98 1532 REPORT NO .... 2 .... SHEET_ ~ OF SUBJECT BETHEL ROAD SEWER LINE BACKFILL REPAIRS COPPELL, TEXAS UTILITY TRENCH BACKFILL OBSERVATION SANITARY SEWER LINE L;UI~VI: NC,). v 179 ;TAi'2&'~7~ 3.0 NUC 120.0 12.5 124.1 11.7 100.1- JOB-NO:IS32 ~TA. 26+70 L;U~VI: NM. v 180 ...... 2.5 NUC 120.0 12.5 119.5 14.2 1 O0 ]OBT, ICXT~32 ~A. 26+80 ~',URVE NO. 9 181 2.0 NUC 120.0 12.5 118.5 13.9 99 JOBNO-.1532-- ~TA. 26+75 ~,URVE NC). 9 182 1.0 NUC 120.0 12.5 122.7 9.7 100+ JOBNO'.'1532 ' ~TA. 26+75 Z. URVE NO. 9 183 ......... .75 NUC 120.0 12.5 120.2 11.8 100 ]OBNOT1532 ~ETEST OF TEST NO. 178 :z ~URME NO. 9 178A NUC 120.0 12.5 121.3 11.3 100+ }OB-NOil$'32 iTA. 25+30 ,'~URVE NO. 9 84 3.5 NUC 120.0 12.5 119.7 11,5 100 JIOBNO:15'32 ~TA. 25+35 ~URVE NO. 9 85 2.5 NUC 120.0 12.5 119.5 10.8 100 ]O-B t~O:1S32' 1 BELOW ASPHALT 2 95% OF ASTM D 698 REQUIRED TYPE OF COMPACTION EQUIPMENTAND NO OF UNITS: ~MM 2210 SHEEPSFOOT VIB~TORY DRUM ROLLER MOFSTURE ~RED BY ~ICKNE~ OF LIFT ~ INCHES JOH~.DEE~E T~CTO.~. (~1 ........ THIS REPORT PRESENTS OPINIONS FORMED AS A RESULT OF OUR OBSERVATION OF FILL PLACEMENT AS WELL AS THE TESTS SHOWN ABOVE, WE HAVE REUEO UPON THE CONTRACTOR TO APPLY THE NECESSAF, N COMPACTIVE EFFORT AND MOISTURE TO ACHIEVE SPECIFIED COMPACTION DURING TIMES WHEN OUR OBSEP3/ER IS NOT PRESENt AND AT LOCATIONS OTHER THAN THOSE TESTED. TEST DATA ARE NOT THE SOLE BA~IS FOR OPINIONS ON WHETHER THE FILL MEETS SPECIFICATIONS. PROGRESS REPORT AS REQUESTED, PBT MADE A SITE VISIT TO OBSERVE AND TEST THE UTI~ RECONSTRUCTION. BACKFILL MATERIAL WAS PLACED IN THE TRENCH BE1WEEN STA, 2,~ 5TA. 25+60 APPROXIMATE 8" THICK LIFTS AND WAS ROLLED UNTIL A MINIMUM OF 100% COMPACTION WAS OBTAINED.