Loading...
SS9402C-LR 980709Compaction Test Report Patton, Burke & Thompson 10555 Newkirk Street Suite 530 Dallas, Texas 75220 CLIENT: CI1Y OF COPPELL 225 PARKWAY BLVD. P. O. BOX 478 COPPELL, TEXAS 75019 DATE 07/09/98 1532 26 JOB NO SUBJECT BETHEL ROAD SEWER LINE BACKFILL REPAIRS COPPELL, TEXAS UTILITY TRENCH BACKFILL OBSERVATION ,TA. ,3,3+7,5 ;..;UNVI: N~O. ! 169 ............... 2.0 NUC 123.0 11.5 125.7 9.0 100+ 10BN0:1532 5TA. 34+50 L:.UNVI: NO. / 170 2.0 NUC 123.0 11.5 122.5 8.0 100 IOBNO11532 ~TA. 34+80 =UEVE no. 7 171 ........ 1.5 NUC 123.0 11.5 124.3 8.7 100+ IOBNO:'T532 ~TA. 33+60 :URV~: NO. 72 1.5 XlUC 123.0 11.5 123.9 10.6 100+ IOBNO~T532 iTA. 33+80 :URVI: NO. 7 73 .75 slUC 123.0 11.5 124.4 11.1 100+ [OB~:1532 iTA. 34+60 :URVE NO. 8 174 ...... .75 XlUC 18.0 14.0 19.1 10.7 100+ lOB'NO, TS32 1 BELOW ASPHALT SPECIFICATIONS[- ! 0~0___ _ 'Yo OF MAXIMUM ~STM D 698 MOISTURE WITHIN % OF OPTIMUM TYPE OF COMPACTION EQU~PME NT AND NO. OF UNITS: CASE 1102 SHEEPSFOOT VIBRATORY DRUM ROLLER CAT CP433-C SHEEPSFOOT VIBRATORY DRUM ROLLER MOISTURE ADDED BY THICKNESS OF LIFT ~ INCHES IYPE OF EARTH MOVING EQUIPMENT AND NO OF UNITS: JOHN DEERE TRACTOR THIS REPORT Pr~ESE NTS OPINIONS FORMED AS A RESULT OF OUR OBSERVATION OF FILL PLACEMENT AS WELL AS THE TESTS SHOWN ABOVE. WE HAVE RELIED UPON THE CONTRACTOR TO APPLY THE NECESSARY COM PACTIVE EFEORT AND MOISTURE TO A~HIEVE SPECIFIED COMPACTION DURING TIMES WHEN OUR OBSERVER IS NOT PRESEN~ AND AT LOCATIONS OTHER THAN THOSE TESTED TEST DATA ARE NOT THE SOLE BASIS FOR OPINIONS ON WHETHER THE FILL MEETS PROGRESS REPORT AS REQUESTED, PBT MADE A SITE VISIT TO OBSERVE AND TEST THE UTILrJ~..~ ,. , .: ~. RECONSTRUCTION. BACKFILL MATERIAL WAS PLACED In THE UTILITY TRENCH BElWEEN~ ~7+~ ~ 35~30." EACH LIFT OF MATERIAL WAS APPROXIMATELY 8" THICK AND WAS ROLLED UNTIL A MINIMUM OF 100% COMPACTION WAS OBTAINED.