Loading...
SS9402C-LR 980609Compaction Test Report Patton, Burke & Thompson 10555 Newkirk Street Suite 530 Dallas, Texas 75220 CLIENT: CITY OF COPPELL 225 PARKWAY BLVD. P. O. BOX 478 COPPELL, TEXAS 75019 CATE: 06/09198 JOB NO 1532 REPORT NO 2 SHEET 1OF~_ SUBJECT BETHEL ROAD SEWER LINE BACKFILL REPAIRS COPPELL, TEXAS UT1LITY TRENCH BACKFILL OBSERVATION LABORATORY FIELD TEST DEPTH TEST MAX OMC DRY MC COM- THIS REPORT PRESENTS OPINIONS FORMED AS A RESULT OF OUR OBSERVAtiON OF FILL PLACEMENT AS WELL AS THE TESTS SHC~/VN ABOVE WE HAVE RELIED UPON TH E CONTRACTOR TO APPLY THE NECE~ COMPACTIVE EFFORT AND MOISTURE TO ACHIEVE SPECrFIED COMPACTION DURING TIMES WHEN OUR OBSERVER IS NOT PRESEN~ AND AT LOCATIONS OTHER THAN THOSE TESTED TE ST DATA ARE NOT THE SO£E BASIS FOR OPINIONS ON WHETHER THE FILL MEETS SPECIFICATIONS PROGRESS REPORT AS REQUESTED, PBT MADE A SITE VISIT TO OBSERVE THE REMOVAL OF THE REMAINING ASPHALT ANq CE~N]'~_ ~E, ~,]I'IE F. Ab'T BOUND ~ OF BETHEL ROAD. mE CONTRACTOR BEG~ ~~l' ~ I~-~ ~D TO $1'A. 1 -I-25. THE EXCAVATED MATERIAL CONSISTED OF A LIGHT BROWN AND RED-BROWN CLAYEY SAND WHICH WAS IN A VERY LOOSE AND DRY CONDmON. SOME PVC AND METAL PIPE WAS UNCOVERED DURING THE EXCAVATION OF THE ORIGINAL TRENCH. THREE PROCTOR SAMPLES WERE OBTAINED AND RETURNED TO THE LAB FOR TESTING.