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Freeport NIP(8.0)-LR040924ineers 8908 Ambassador Row, Dallas, TX 75247 2696 Gravel Drive, Port Worth, TX 76118 6300 Rothway, Ste. 150, Houston, TX 77040 Corporate Phone: (214)630-9745 IN-PLACE DENSITY TESTING Client: Project: Duke Realty Services, LP Mr. Brian Straley 5495 Belt Line Rd., Ste 360 Dallas TX 75254 J Freeport XI & XII Coppell, Texas Services: Perform In-Place Density Test in accordance with ASTM Standards. CONTRACTOR: Duke Construction Test Methods: ASTM D-2922 ASTM D-3017 PROJECT DATA Gauge: Troxler 3430 Moisture Gauge Serial No: 35518 Current: 704 Test Mode: DT Previous: 739 Report No.: 217385 Project No.: 049245 Date of Service: 09/01/2004 Report Date: 09/24/2004 Standard Counts Density Current:. 2683 Previous: 2725 M/D No. Description MOISTURE DENSITY RELATIONS Maximum Moisture % Density pof Project Requirements Moisture Density 1 Brown Silty Sandy Clay 20.0 103.0 Optimum +4 95 min FIELD DENSITY TESTS TEST PROBE NO TEST LOCATION DEPTH Utility backfill 1 Storm drain, west side, Station 1+75, 1' 6" below grade Utility backfill 2 Storm drain, west side, Station 1+75, grade 6" Utility backfill 3 Storm drain, west side, Station 3+75, 1' 6" below grade Utility backfill 4 Storm drain, west side, Station 3+75, grade 6" Utility backfill 5 Storm drain, west side, Station 5+75, grade 6" Utility backfill 6 Storm drain, west side, Station 7+00, grade 6" M/D MOISTURE WET DENSITY DRY DENSYrY DENSITY No. (%) (pcf) (pcf) (% max) 1 20.9 118.8 98.3 1 21.0 118.1 97.6 I 20.0 119.4 99.5 r 95 95 97 1 21.6 120.4 99.0 96 1 21.7 120.4 98.9 ~_96 1 22.9 120.2 97.8 95 LIMITATIONS: The test results presented herein were prepared based upon the specific samples provided for testing. We assume no responsibility for variation in quality 07SS Page 1 of 2 RoneEngineers Report No.: 217385 Project No.: 049245 Client: Duke Realty Services, LP TEST NO TEST LOCATION ]PROBE DEPTH M/I) MOISTURE WET DENSITY DRY DENSITY DENSITY NO. (%) (pcO (pod (% max) Utility backfill 7 Storm drain, west side, Station 7+00, grade Utility backfill 8 Storm drain, east side, Station 0+50, 1' below grade 6" 1 21.9 120.4 6" 1 21.5 120.0 Technician: Joe Jernigan Report Distribution: (1) Duke Realty Services, LP (1) Exiranet (1) Cit~ of Coppell (1) City of Coppell 98.8 96 98.8 96 Test results on this report meet project specification. ~ ~ Started: ll:30a Finished: 12:45p Ro~/~ K. Scott Watson, AET CMT Operations Manager LIMITATIONS: The test results presented herein were prepared based upon the specific samples provided for testing. We a~sume no responsibility for variation in quality Page 2 of 2