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ST9302-CS 980311SANDY LAKE - FROM DENTON TAP TO MACARTHUR BLVD CATEGORY NUMBER OF L.F, CONST. LOWER/RELO $ 1. PAVING 6 3,300 1,131,900 CONFLICT 2. DRAINAGE .~ "~ 150 93,000 CONFLICT SHUTDOWN PERIOD - ])AYS 14 8 3. STREET LIGHT 17 595' 368,900 FOUNDATION CONFLICT The existing design requires paving, drainage and streetlight foundation conflicts. lowering the entire limit of 10, 160LF at a cost of $2.6 M. The ori~nal 7 section lowerings of 5,370 LF, based on the project report dated 7/21/94 account for paving and drainage conflict, however requiring a minimum cover of 8 FT. the standard air valve design. NOTES AND ASSUMPTIONS: PAVING: 1.. The 6 section lowerings are at the following station (Paving Conflicts): due to 66 ooo 1.1 8+75 to 12+25 -- 350LF 20+50 - New air valve installation to replace the existing AN 1.2 29+25 to 33+50 = 425LF 43+00 - New air valve Installation to replace the existing A/V 1.3 68+50 to 74+40 = 590LF 1.4 79+25 to 86+50 = 725LF 1.5 95+00 to 100+00 = 500LF 1.6 100+90 to 108+00 = 710LF Total = 3,300 LF ~ $343/LF, consisting of 17 bid items based on current prices Page 1 of 3 @ 2. The shutdown period estimate was based on factfinding conversations with Johnson Bar Contractors, in-house design and construction personnel and a meeting with Distn"o~ Division. Reference attached memo to M. Riehman 3. New air valves will be installed at sta. 10+50, 20+50 (re-install), 33+00, 43+00(re and 714-00. The new A/V system each will cost $16,000. incl. 2 manholes.. 4'. A new configuration for the Air Valve system will be utilized to minlmiTe cover reqt to only 3.8 Ft. This Air Valve design was first installed in the Denton/Rossford project ex. 66" main in 1997. Brothers, ion irement on the 5. Prior to tie-in, a total of 200,000 gal. dewatering will be accomplished wi~ the in~ation 0fblow-offvalves at low points. Note: Do not use greater than 1300 GPM diseharge ~or the pump.. ' ~ 6. Two existing air valves not included in the lowerings will 'be re-installed using the ne~v A/V design. DRAINAGE: 1. The 3 drainage conflicts are at station:  03, 21 RCP (1Ft. dire, et conflict) - Redesign nmy be possible~,'~' . 19, 2I"RCP (4"clearance) - Redesignmaybeposs~ble~'-cx~.,~e-' +40, 66"RCP (4FT. Direct conflict).-redesignLowering may be required or need major 1 +17 - Direct conflict with 27"RCP - Lowering no. 6 was extended by 110 LF accommodate this conflict and one strcc4 foundation conflict -31 000 Estimated Cost: $ , /lowering~consisting of a total of 150LF pipe~ 300/LF and 6 closures ~ $$,000 each Page 2 of 3 STREET LIGHT FOUNDATIONS: The proposed street light 24" drilled shafts approximately 8 Ft. deep are in conflict at 24 different locations. However, 7 of these conflicts will be cleared in conjunction with the lowerings in item #1, leaving 17 conflicts to be cleared at the following stations: 1. 7+22--- ' '~-.14+92- ~ 4. 24+89 5. 27+94 6, 36+72 7. 38+20 8. 39+76 ~ ~ 42+75 '~M0. 49+18 12. 56+11 14. 60+80 ---~ 15. 64+20~> 16. 67+60 -- 17. 94+64 --'7 Estimated Cost: GENERAL NOTES: $620/LF ( 35LF per relocation, total 595 LF) 2OOo 1. Special Provisions will be included to protect the existing main from heavy equipment during grading operations. Minimum 2.0t~. cover will be maintained to not allow total e: capacity to exceed 6600g/ft. Sheepsfoot rollers will not be permitted; skid boar& will b installed to distribme the load, etc. 2. Design Services estimates approximately 4 weeks to complete in-house design for the 6{ lowerings. Jun Battad - 3/09/98 Page 3 of 3 x