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CF-Justice Center-LR060918 In-Place Soil Moisture/Density Tests by Nuclear Method eM J ENGINEERING, INe. 7636 Pebble Drive Fort Worth, Texas 76118 Tel: (817) 284-9400 Fax: (817) 589-9993 Client: Project: Harrison, Walker, & Harper Police and Fire Renovation City of Coppel! Report Distribution: (1) Harrison, Walker, & Harper (1) City of Cappel! (1) Brinkley Sargent Architects (1) Structural Engenuity (1) Teague, Nail, & Perkins -------- ------------------ --------------------- ---------------------------- CMJ Report No.: 875-6111-006 Report Date: 09/18/2006 Specifications Percent Compaction: +95% min Moisture Content: opt +0% to +4% ** REVISED REPORT ** see Additional Remark(s) below: Test Data Date Tested: 08/31/2006 Technician: Phil Sommerville Curve No. Test Method Material Description Optimum Maximum Dry Moisture % Density pet 2777 2756 ASTM D-698 ASTM D-698 Dark Brown and Gray Clay Grey Sandy Clay w/Some Organics 20.5 99.0 14.0 113.0 In-Place Test Results Test Elevation Ref. Probe No or Lift Location Curve Depth 8" Waterline 5.1 -1' BFG 40' West of East 45 degree Bend 2777 6" 6.1 -1' BFG 10' North of Existing Curb at 10' East of 2777 6" East 45 degree Bend Trench Utility Backfill 7.1 -2' BFG Retest of #7.0, Report #875-6111-003 2777 6" 8.1 Final Retest of #8.0, Report #875-6111-003 2777 6" Percent Wet Density Dry Density Percent Moisture (pct) (pct) Density 23.8 122.2 98.7 99.7 21.6 119.7 98.4 99.4 24.0 119.4 96.3 97.3 23.1 120.3 97.7 98.7 Test results on this report meet project specification. Test Method(s): ASTM D2922, ASTM 03017 Additional Remark(s): {BFG} Below Final Grade 7.1 and 8.1 Retest of Report #875-6111-003; Date Tested: 8/24/06 5.1 and 6.1 Retest of Report #875-6111-003 Date Tested 8/24/06 ** Revised Report from original Report dated 08/31/06 note changes of test numbers 11 and 12 to retest numbers 7.1 and 8.1 Gauge: CPN Gauge SN: 6430 Std. Density Count: 42465 Std. Moisture Count: 8944 CMJ Engineering, 'nc R. Car' Lee, S.E. T. Vice President/CMT Manager LIMITATIONS: The test results presented in this report apply only to the specific samples, items, and areas described within this report. The test results do not pertain to any other samples, items or areas regardless of similarity. Our reports are produced solely for the exclusive use of our client. This report or any portion of this report may not be reproduced without the written consent of our client and CMJ Engineering, Inc. 07 Page I of I Cancellation Report eMJ ENGINEERING, INC. 7636 Pebble Drive Fort Worth, Texas 76118 Tel: (817) 284-9400 Fax: (817) 589-9993 Client: Project: Harrison, Walker, & Harper Police and Fire Renovation City of Coppell Report Distribution: Harrison, Walker, & Harper City of Coppell Brinkley Sargent Architects Structural Engenuity Teague, Nail, & Perkins CMJ Report No.: Date Tested: Activity: Technician: 875-6111-013 September 18, 2006 Drilled Pier Excavation Larry Smallwood On Monday, September 18, 2006, the above technician, representing CMJ Engineering, Inc. arrived on-site at 8:00 a.m. as scheduled to observe drilled pier excavation. Upon arrival, the technician was informed that drilling operations were cancelled due to rain. CMJ Engineering, Inc. R. Carl Lee, S.E.T. ice President/CMT Manager The test results presented in this report apply only to the specific samples, items, and areas described within this report. The test results do not pertain to any other samples, items, or areas regardless of similarity. Our reports are produced solely for the exclusive use of our client. This report or any portion of this report may not be reproduced without the written consent of our client and CMJ Engineering, Inc.