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Town Center L1B2-LR 991201CONCRETE COMPRESSIVE STRENGTH TEST fBC ENGINEERING, INC. 8901 Carpenter Frwy., Suite #100 Dallas, Texas 75247 Report No.: 9931189 Report Date Date of Service: 11/19/1999 12/01/1999 Client No.: 26295000 Client: Ewing Properties, Inc. Attn: Mark Morris 14990 Landmark Blvd, #300 Dallas TX 75240 -6729 Project No.: 94991134 Project: Tom Thumb Denton Tap & Sandy Lake Coppell, Texas Services: Obtain samples of fresh concrete at the placement locations, perform required field test and cast compressive strength samples. PROJECT DATA CONTRACTOR: Hill & Wilkinson CONCRETE SUPPLIER: Lattimore PLANT: 7 SPECIFICATION REQUIREMENTS STRENGTH: 3000 psi @ 28 Days SLUMP: 4.0" Max AIR: N/A TEST METHOD: ASTM C -143 7 ASTM C -172 3.50 ASTM C -39 CONCRETE CLASS: 17 PLACEMENT DATE: 11/19/1999 BATCHTIME: 11:24am TIME SAMPLED: 12:14pm BY: Joey Gordon WEATHER CONDITIONS: Clear TEMPERATURE (F) - AIR 76 F CONCRETE: 82 F TRUCK NO: 1040 TICKET NO: 708164 AIR CONTENT ( %): N/A UNIT WEIGHT (pcf): N/A PLACEMENT LOCATION: Slab -on- grade /entrance to front door 15' from front door, 15' north and south of door SAMPLE LOCATION: 6' from front door & 3' N of -door CYLINDER MEASURED 125500 4440 MARKED SLUMP DATE AGE SET NO. (inches) TESTED (days) 1 1 3.50 11/26/1999 7 1 2 3.50 11/26/1999 7 REPORT OF TESTS ACCUMULATIVE YARDS: 10 MAXIMUM COMPRESSIVE LOAD STRENGTH (tbs. force) (psi) 130600 4620 125500 4440 Average 4530 FRACTURE TYPE 1 3 3.50 12/17/1999 28 1 4 3.50 12/17/1999 28 Sampled from truck, tailgated. Technician: Joey Gordon started: 10:30am Finished: 1:30pm JL X- ^ - , Engi , Inc. Report Distribution: (l) Ewing Properties, Inc. (1) Raymond L. Goodson, Jr. Engrs. (1) S.0 Companies (1) Hill & Wilkinson, Inc. Eugene Harbour (1) Tom Thumb Stores Division (1) City of Coppell - Engr. Dept. Vice President (1) Michael F. Twichell, Inc. This report is exclusively for the use of the client indicated above and shall not be reproduced except in full without the written approval of HBC Engineering, Inc. O1LL Page 1 of 1