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Town Center L1B2-LR 990729IN -PLACE DENSITY TESTING f 19C ENGINEER U, INC. 8901 Carpenter Frwy., Suite #100 Dallas, Texas 75247 Date of Service: 07/14/1999 Client No.: 26295000 Client: Ewing Properties, Inc. Attn: Mark Morris 14990 Landmark Blvd, #300 Dallas TX 75240 -6729 Services: In -place density testing. Report No.: 9919120 Report Date 07/29/1999 Project No.: 94991134 Project: Tom Thumb Denton Tap & Sandy Lake Coppell, Texas PROJECT DATA CONTRACTOR: Hill & Wilkinson MOISTURE DENSITY RELATIONS: MM N o. Description Laboratory Test Method: ASTM D -698 Field Test Method: ASTM D 1557 ASTM D -2922 Maximum Mo i s ture % Dens p ct Project Requirements Moisture Density 1 Reddish brown sandy clay 19.5 105.0 -143% 95% FIELD DENSITY TESTS TEST M/D MOISTURE DRY DENSITY DENSITY NO TEST LOCATION No. (pd) (% ma 4 " Sanitary Sewer 114 Final lift, Station # 0 +50 1 18.9 102.1 97 115 1st lift, Station # 0 +50 1 19.4 101.7 97 Test results on this report meet project specification. NOTE: Sewer line is not shown on plans, line runs from 8 inch sewer line to grease trap at N.E. Corner of existing building. Station 0 +00 starts at grease trap. Technician: Roy Montgomery En ine ng, Inc. Report Distribution: (1) Ewing Properties, Inc. (1) Raymond L. Goodson, Jr. Engrs. (1) S.0 Companies (1) Hill & Senior Wilkinson, inson, Inc. eni D. Smith, P.E. (1) Tom Thumb Stores Division (1) City of Coppell - Engr. Dept. or Project Engineer (1) Michael F. Twichell, Inc. This report is exclusively for the use of the client indicated above and shall not be reproduced except in full without the written approval of HBC Engineering, Inc 07TMP Page 1 of 1